Another busy day
Posted: Sun Oct 31, 2010 1:51 pm
I received a call from our DBS locomotive control saying that the 6B13 petrol tanker train from Milford to Westerleigh , Bristol had set of an impact detector, with luck I was working on a locomotive as it came past me.I had to close the relief good line and inspect the first 100 tonne petrol tanker wagon behind the train locomotive.The wheelsets were badly damaged and could not continue its journey.I then had to shunt the wagon off the train to the adjacent yard.To make things worse,we had to contend with a points defect preventing me doing this job.After a wait of 45 mins,the delicate operation was carried out.After a delay of over one hour,the train got on its way after I had carried out a brake test.
The photo shows the train on its way again driven by Duane Curtis,who owns a London bus and is also interested in machinery.
Martyn
click on photo to enlarge,Duane looks cool with his top gun sunglasses
The photo shows the train on its way again driven by Duane Curtis,who owns a London bus and is also interested in machinery.
Martyn
click on photo to enlarge,Duane looks cool with his top gun sunglasses